![]() ![]() My main point is that it worked well before flashing new FC firmware. If the quad does arm, then the motors don't respond in unison. I am trying out new firmware at this point. But I am having issues getting all the motors on the same track, and sometimes arming the quad is not working. Regretfully, I did not save the state that the FC was in before flashing new firmware.Īny clues of where I could have gone wrong? And how to fix this? but then again, I can see the RX on my transmitter display. It seems the transmitter is not binding with the receiver correctly since I'm reading no values on Cleanflight. when I try to read values under the "receiver" tab on CleanFlight, I get nothing. I can confirm with "RX" symbol in the corner of my transmitter display. I bind the transmitter and receiver again. I flashed firmware to the F3 flight controller, and after that, the FlySky doesn't seem to work anymore. I needed to calibrate everything using CleanFlight, which resulted in updating the firmware. ![]() ![]() Turns out the issue was a faulty mini USB cable the whole time.īefore updating the firmware, my quad would arm and run just fine. I had quite the ordeal figuring out how to update the firmware of my SPF3 FC. ![]()
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